Tuesday, December 31, 2019

Cold start-up



Points to Remember
Ø  maximum of HP casing and HP shaft is less than 150°C(more than 5 days)
Ø  It requires soaking of Turbine at 360 rpm with steam(40ksc,360 Deg)
Ø  An upper limit of 200° C/hr. saturation temp gradients can be allowed, i.e. approximately the boiler pressure can be brought to 20 Kg/ Cm2 within an hour of cold start up
Ø  But actual temp gradient is limited by the thick walled Y piece provided in the main steam and HRH lines
Ø  maximum differential temp allowed between inner (98%) and mid wall temp (50%) is ±40°C
Ø  Start only two CC pumps in order to minimize flashing in down comers (and subsequent vibration) when the boiler water is in the range of 85° to 125° C
Ø  third pump should be started before drum pressure reaches 7 Kg/Cm2 to minimize the temperature transients experienced by the pump casing ( this is to avoid fast load out back on the boiler in the event of any CC pump tripping).
Ø  To get the rolling parameters, normally two elevation oil guns are taken with approx. 70 to 80 t/hr. flow through HP-LP bypass. At that time MS parameters would be 40 Kg/Cm2 and 360° C.
Ø  As soon as the turbine loading has started, HP/LP by pass closes
Ø  First mill is put into operation around 10% of generator load
Ø  Second mill is put into operation around 25%
Ø  Third mill at 40% of generator load
Ø  Fourth and fifth mills are put into operation at 60% and 80% of generator load respectively
Ø  Sixth mill is taken to reach full generator load
Ø  During loading the RH outlet steam temperature has to be kept as close as possible to SH outlet steam temp. Burner tilt, SH spray, RH-spray controls have to be adjusted accordingly
Procedure
SNo
Time
Condition
Action
Follow-up
Status
1

0 ksc
Charge PRDS from other Units (14ksc,>260 Deg)
Open drains at PRDS,TG Floor,8.5 m




Charge Atomizing steam(Pr 6.5 ksc)
Open drains at 4 elevation

Fill Water upto +200 mm
One CEP i/s
LPH,HPH charged from FW side
Deaerator Level =175 mm
Hotwel b/w -100 to -200 mm
FRS 30 % to fill Drum /load upto 180 MW
Drum, SH, RH Vents , SH Drains : Open
LPD : Drains Closed
BSV : closed
Drain Before BSV :Closed
MS strainer drains UFT/SDFT: Open
HRH strainer Drain UFT/SDFT : Open
ECO Recirculation E20 Manual : Open

Charge LDO upto HOTV


ESP ready in charge Condition
Open i/l, o/l damper of passes

Bottom Hopper & Seal Trough Lined-up


EAST, Excitation panel, GRP Panel Ready


Generator gas Pr= 3.5 ksc


H2 cooler,PW system Ready


Start one CC pump
Drum >+200 mm, Vents B3,B4,B5,B6 Closed

Start second CC Pump
Drum normal =+50 mm, B3, B4,B5,B6 Closed

Start Scanner Fan


Start Both SAPH
Air Motor availability to be checked
FG/Air Inlet/Outlet Dampers Open

Start Both PAPH
Air Motor availability to be checked
Air Inlet/Outlet Dampers Open
FG Inlet/Outlet Dampers closed

Start one set ID/FD, Air>30% (600 TPH)
SADC 100 % (auto)

Charge SCAPH for Running FD Fan
Check for Increase in Air Temp at SAPH i/l

Start Purge (Duration :  5 min)
HOTV, LOTV got reset
SADC will released from 100 % in auto

Machine on Barring
LO Temp=45 Deg, Speed=80-100 rpm
JOP Header Pr=140 ksc
Start MOT Centrifuge
HPCF Charged, Temp=55 Deg





2




0'
Boiler Ready & turbine on Barring
Start 4 guns in AB elevation


 After 30', Start 4 guns in CD elevation
To match Drum MTM Raise 2 Deg/Min
LDO control Pressure =9 ksc
Start : Pair AB 1/3 and after 7 sec AB 2/4
Check scanner Intensity / Local Verfied
Start : Pair CD 1/3 and after 7 sec CD 2/4
Open E20 R/C valve, if MDBFP not feeding in Drum
Check Drum Level/ Open CBD
Check D/A Level & H/W level

Start GSC Exhauster fan
Charge Seal steam upto Supply Motorized v/v of GS supply  station
Start Vacuum Pumps one by one
Open dtain before NRV
Steam Temp >250 Deg

Drain Casing of Pumps,
Fill Receiver tank >80 % in VG

At -0.2 ksc, charge seal steam
By bringing controller from 50 % towards zero
Build Vacuum upto -0.9 ksc

Open HPBP Warm-Up drains


Switch on SLC Drains
Verify: Manual v/v  Opened

3
60'
Drum Pr= 2ksc
Close SH/RH Header Vents
Close SH Header drains at Dr Pr =10 ksc
Open BSV Bypass Lines


To Warm up Ms/CRH/HRH lines

4
100'
Drum Pr= 5ksc
Open LP Bypass 10%
Open BSVs
Open HPBP by 10% at Dr Pr=7 ksc
Start 3rd CC pumps at Dr Pr=9 ksc
Take Additional EF gun ( If Required)
Close HPBP Warm-up valves


Open 1st HPBP Warm-up valves
Close CRH drain Pot at TG 0m




Rolling through SGC


5
150'
MS =15 ksc/
180-200 Deg
HRH=8 ksc
Switch On start-up Sequence of SGC-turbine

TSE Influence comes ON


6
300'
MS =50  ksc/
350 Deg
HRH=8 ksc/350 Deg
Turbine Ready to Roll
Turbine Speed raised to 360 rpm through SGC sequence
Ensure LO TCV on auto with SP=45 Deg
Gas Controller on auto
PW controller on auto
Ensure closure of Barring valve at 240 rpm
Monitor TG Vibrations, TSI, Bearing Temp
MS Pressure/Temp to be maintained upto load 50 MW


7
360'
MS =50  ksc/
350 Deg
Turbine at 360 rpm
Turbine Speed raised to 3000 rpm through SGC sequence
Check X6 criteria
Ensure Tripping of JOP at 540 rpm
Ensure Tripping of AOP at 2950 rpm


8
370'
MS =50  ksc/
350 Deg
Turbine at 3000rpm
Switch Off SGC Program
Put AVR on auto
Close Field Breaker
Select Main GCB
Switch on Synchroscope after select Check
Synchronise unit through synchroscope from OWS
Raise Speed SP by 15 rpm
Close MAL drains and other HE drains
Check X7 criteria

GT Cooler Fan starts on auto/ Verify

Load Ref=50 MW . Pr Max=75 MW
Turbine Speed will Decrease

9
390'
Load=55 Mw
MS Pr=54 ksc/350 Deg
HRH=12 /340 Deg
Start PA Fan, Seal air Fans starts in auto
Take 1st Mill
Start 2nd set of ID/FD Fans
Cut in LPH-2, 3
Cut out Deaerator steam from PRDS
Peg Deaerator form CRH =2 ksc
Cut in all controllers
Open PAPH FG/Air inlet/outlet Damper Open
PA Header Pr=800 mmWC,
SA Disch Hdr=1500 mmWC



10
420'
Load=
110 MW
MS=70ksc/370 Deg

Charge PRDS from CRH
Peg D/A upto 4ksc( gradually)
Cut in 2nd Mill
Start withdrawing Oil support
Control MS/HRH Temp with Burner Tilt  and spray(if Required)

Ensure energizing of Trim Device at 100 MW load


Ensure Fireball scanners Healthiness

11
440'
Load=
160 MW

 Rest as per Hot/Warm start up



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